The tune sounds perfectly mint in that video.
I was going to ask if you made sure the ignition timing was calibrated (what the FAST thinks it's running, is verified with a timing light) but it just sounds too healthy to be that.
Bad luck with parts or assembly maybe? the thing just sounds perfectly happy...!
Yeah..we check with light. Last few years we didn't record timing becase of the limited recording time of the FAST data
logging but we put it in this year to check. Rob Frey said there was a unit from FAST for more time.
Still haven't found what caused the rod to fail but Dry sump was empty. All rods move on crank, including #6

and crank looks unscored with 3/4 of cap still on ratteling on there with no bearings in it.
These engines can run on splash for awhile. Troy got into the El Mirage 2 club in 1990 at 229+ and me at 206 in high gear
only when shift lever broke at start line [ long push but pulled right away]. We then went to Bville and had a 275 exit speed
with 2 push rods worn out hardly opening the valves. On return record run rod blew side of our not new repaired block and
part of the oil galley showing the copletly welded up oil galley. Bearings had been inspected several times showing no problems but the rockers get oil from passage up from the last main bearing causing our lifter problem. Rods 6- 7 and 8 and last main were getting no oil

When Bvillercr has time [ a week or so from now] we'll take video of data log and post it.
Congrats on taking our record. Records mean more with competition and we look forward to getting it back
JL222