I believe Cory told me a floater came apart in the clutch, jammed in the bellhousing, the motor kept churning, things started welding, then it stuck and sheared the bell off the motor.
Car sounded great on the runs, Les got the car stopped well with both problems, Marlo wanted to see a parachute test at 400, that was the purpose of the trip. Of course a time slip with a 475 - 5xx would have been spectacular.