Actually our biggest concern is keeping the flywheel on the crank and not so much blowing it up. The achilles heel of the stock crank is the flange and we've cut a few motors in half after the flange breaks and the crank free revs to 7000 rpm or so and all the rods let go and take out the block. Yeah, we don't like it when that happens.
^^Well I hate to sound like a pessimist but I am a realist and can't hope for something that I know isn't going to happen. Our biggest concerns wound up materializing for us yesterday when the flange broke off the back of the crank at the end of a WOT pull. But not all was lost... absolutely not. At a minimum we learned a LOT plus we were hitting our power target which was very affirming. So here's how it went...
We did some initial tuning on Friday after work and by time we had called it wraps for the night we were already making half throttle power pulls and seeing good results. Surprisingly, it didn't take quite as much time to get the injector phasing and advance stuff dialed in. It's by no means dead-on perfect but I think it's a hundred times better than before so it seems like just having sequential fuel delivery made a huge difference by itself. I'd say our proof of concept has been validated.
On Saturday morning we started right back at it again bright and early and it wasn't long before we got into doing WOT pulls. We had bought 10 gallons of the 101 octane unleaded gas that ERC has at the June El Mirage meet thinking it was more than we would need. Well we wound up running out about mid day and had to get something to keep going. Luckily I knew of a place near by that was a VP dealer so we picked up 5 gallons of their 100 octane "street blaze" gas. Oh boy did changing the gas make a huge difference - for the worse. It was running really sweet on the ERC gas and it sounded fat and blubbery on the VP but I made some changes to the fuel map to compensate and we carried on.
The goal was 150 crank hp. Working backwards from our power goal, I figured on 10% drivetrain loss and the Mustang dyno we were tuning on reads absurdly low... like 15-20% low. A known 400 hp car will come to our dyno and make 300 whp. Anyways, so 150 hp would be 135 hp to the wheels minus 20% power on the heart breaker dyno puts us at 108 whp and we were making 110 whp very consistently. We were like "wow, we're actually doing what we wanted to do... cool." I was trying to get the AFRs dialed in a little better on the top end and then BANG, the flywheel broke loose. All of a sudden there was lots of black smoke and sparks and a whole lot of noise and then it was quiet... very quiet.
After it was all said and done I went back through and counted all my data logs and there were 47 and I know I didn't log every single run so we had some 50+ runs on this motor before the crank let go. Honestly, I'm glad it happened on the dyno and not on our first pass down the track or on record runs or something. What usually happens in this instance is what I described in the quote above; the crank free revs to some absurd rpm and then the rods let go and we totally destroy the motor. Well this time it revved to about 6000 rpm and then the limiters kicked in and kept it from going higher so all the rods are still inside the block and hopefully not hurt.
It looks like Speed Week is out for us this year. I think after breaking who knows how may cranks we're finally done screwing around with stock crankshafts. They are just too much of a liability to even mess with once you're making this kind of power. We don't exactly know what our next step is but we want to get back at it soon.
Here are some vids from the dyno. Sorry about them being so short; I had someone else working the camera.
VIDEO 1 Eeeehh this was a camera test. Oops.
VIDEO 2 Running it up through the gears. The o-scope is showing you a clue to our key tuning point.
VIDEO 3 WOT pull to 5000 rpm. The smoke is water spritzing out of the cracks in the head and onto the headers.
VIDEO 4 Another WOT pull to 5000 rpm; I was getting a shower standing over there.
VIDEO 5 Partial pull; I had figured the alternator wasn't working when my battery volts at idle was less than 12. Well it was confirmed when the voltage dropped below 8 volts in the middle of this run and everything started to go lean. Shut the motor off then tried to crank it over and all we got was a click. Dead battery. Swapped it out for another one and kept going.
So that's it. Our mule was pretty short lived but it served its purpose and now its legs have fallen off and it can't go any more. We should be able to drop this tune into our next motor and keep going. Things should really start to get fun once we get the turbo back on.